The Build (in review)
I review the components of LoCARB and how they performed after 94 days out in the ocean.
Continue readingHome of the Low-Cost Autonomously Run Boat
I review the components of LoCARB and how they performed after 94 days out in the ocean.
Continue readingLoCARB has its main thruster repaired, its solar system loses a charge controller, and LoCARB gets a backup thruster. Also, LoCARB gets launched again.
Continue readingLoCARB was launched the second time, with some useful software upgrades! Also, credit is due where credit is due.
Continue readingNavigation for LoCARB tested and complete, with a top speed clocked at 2 knots…Not a bad speed for being 125lbs!
Continue readingMonitor a Pixhawk flight controller autopilot with an Arduino using the Mavlink protocol.
Continue readingUse an Arduino to send a mavlink message to the autopilot to change flight/driving mode.
Continue readingConsolidating electronics and plans for if LoCARB is found
Continue readingFinished programming…I think. Whats next? Building and testing the solar power system and the physical boat hull!
Continue readingA quick update about KST servos, Rockblock Naked MK2 Sat modem, and LOCARBs electronics progress
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